Mitigation Of Loss Circulation Problems Using Calcium Carbonate In Well 'HF-05', 'Kanaan' Field

Authors

  • Heldy Febryanto Sekolah Tinggi Teknologi Migas; Indonesia
  • Firdaus Sekolah Tinggi Teknologi Migas; Indonesia
  • Risna Sekolah Tinggi Teknologi Migas; Indonesia
  • , Abdul Gafar Karim Sekolah Tinggi Teknologi Migas; Indonesia
  • Aprilino Alfa Kurmasela Sekolah Tinggi Teknologi Migas; Indonesia
  • Iin Darmiyati STT Migas Balikpapan
  • Annisa Efidiawati Sekolah Tinggi Teknologi Migas; Indonesia

DOI:

https://doi.org/10.37680/almikraj.v2i2.7211

Keywords:

Loss circulation; Hydrostatik Pressure; Drilling Hydrulics; Calcium Carbonate

Abstract

Lossicirculation isione of theiproblems thatioften occursiin theidrillingiworld where loss of circulation or loss of circulation of mud is interpreted as a loss of circulation in a small amount or all of the drilling mud when it is circulated, so that when the drilling takes place, the circulated mud enters the drilling zone. penetrated formation. The "HF-05" well in the "KANAAN" fieldiis aidevelopmentiwell thatiaimsito proveithe existenceiof oil and gas reserves in Sukra District, Indramayu Regency. The loss circulation problem that occurred in the "HF-05" well occurred at a depth of 1945 mMD, route with a total loss of 278 bbl with a mud weight of 1.19 sg. The methodology used in handling loss circulation is collecting the necessary data, calculating hydrostatic pressure (PH), calculating drilling hydraulics, and identifying the causes of loss circulation by comparing hydrostatik pressure (PH) with formation pressure. Then carry out countermeasures using loss circulation material (LCM) type Calcium Carbonat. The results of countermeasures for loss circulation using loss circulation material (LCM) type Calcium Carboante in the "HF-05" well were successful with hydrostatik pressure (PH) lower than formation pressure (PF).

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Published

2022-06-15